I'll give some brief overviews to some of these pics.
Not full exhaustive build labors.
I have a running parts list i'll post later on that basically covers all that.
Underhood, it was a mess.
Everything came out/off except actual engine and tranny.
And 90% of it was replaced. The rest refurbished. It looks like a brand new rebuilt engine - visually.
The fuel filter was dangling between airbox and fender apron, so i relocated it on the firewall. All fuel hoses are new front to rear. Put clear hoses underhood.
The wiring was going everywhere and took some odd routes.
Straitened it all out and put it all inside plastic wire looms.
Made a battery hold down for the oversize battery that came with it as bought.
Half (or more) of the electricals on Truck were inoperable front to rear. Most all those were easy fixes, once diagnosed (not always easy).
Everything functions properly now - except the wipers don't park themselves at bottom. Probably the relay, but not swapped any to it yet. And I did a manual reverse light toggle, thought it might come in handy. Also added a coolant level sensor/warning system.
Everything about the cooling system was replaced with new, down to the clamps. Except the water pump that the guy had installed when he did the timing belt. Upgraded to Mk2 2spd fan/shorud assembly.
It ran much better with cold start pulled, so i knew he had the timing low. Tinkering - i began advancing the InjPump - until it ran out of adjustment. Basically the pump was 1 tooth off. It ran better and smoked less. Left it like that until after i was finished revamping everything. After all that was done, i set it up right and dialed in on 1.05
Ran much better, started instantly, and the more i drove it the better it got. Until it basically stopped smoking all together.
It does have a funny problem with oil consumption. It eats about a quart every 500 miles. The 2 studs for #1 exhaust port were gone - but looked like gasket was still there. Put in 2 bolts and hoped for best. After the first 200-300 miles it began leaking oil from that exhaust port gasket. And it continues. The only leak on the whole Truck.
But it runs fine, minimal blow-by, rarely puffs any Blue, just ocassionally on some start-ups. So its just gonna be that way. Probably have real bad valve seals. I'm going to build another true TD engine for it anyhow soon. And maybe a FN tranny upgrade.
It has a reman'd 82 CR 12mm engine (unknown miles) with everything from an 85 TD engine swapped onto it - top to bottom including air supply. And the 85 TD 5spd code ACH.
I've put about 3000 miles on it, 1700+ were a roundtrip to Markham Ontario Canada.
Since these pics were taken - have removed the washer reservoir i made from a generic overflow tank and a spare mk2 washer pump. Its been replaced now with good working factory stuff.
Have added a boost gauge. Sourced some plastic strut caps. Sourced Mk1 TD Airbox and Snorkel.
Next little project will soon be mounting up the new control arms, balljoints, steeringlinks, urethane bushings, and a front end alignment.
I averaged 38-39 mpg before going to Canada.
38-39 with LDA boost hose disconnected for 500 miles (waste of time trying out ECO mode).
And 38-39 with about 1200-1500 pounds coming back from Canada.
After the rest of the front end work - hoping to top 40mpg.
The shell offers some resistance to the wind i'm sure.
Probably costs about 3-5 mpg.
Worth every bit of it.