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Author Topic: DIY fix for screwed up crank noses  (Read 22723 times)

April 17, 2008, 09:19:40 am

lord_verminaard

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DIY fix for screwed up crank noses
« on: April 17, 2008, 09:19:40 am »
Figured I would post this here, as apparently this is a common problem with 16v engines that get a serpentine conversion.  This guy has made a jig so you can drill into the crank nose and press in hardened dowel pins to prevent the keyway from shearing off.  Before, this fix required pulling the engine and crank and having a machine shop do the work.

http://forums.vwvortex.com/zeropost?cmd=tshow&id=3793002

Enjoy!  Rob, (the guy who posted the thread) has done a lot of various fabricating for the Scirocco crowd and he really knows his stuff.

Brendan


81 Scirocco 'S -->Soon to be m-TDI
93 Corrado SLC VR6
'86 Golf N/A Diesel  -->Wife's car
1990 Audi CQ
05 New Beetle PD TDI


"I am a man, I can change... if I have to.... I guess....."

-Red Green

Reply #1April 17, 2008, 11:42:36 am

GoKraut

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DIY fix for screwed up crank noses
« Reply #1 on: April 17, 2008, 11:42:36 am »
I also have a little more detailed explanation written up in this thread here:

http://forums.vwvortex.com/zerothread?id=3409003

Here are some pictures of the jig just being used on the cog/sprocket:




Reply #2April 17, 2008, 01:13:38 pm

zukgod1

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DIY fix for screwed up crank noses
« Reply #2 on: April 17, 2008, 01:13:38 pm »
Man what I wouldnt give to have a serp system on my car.. :(
dan

99 Golf TDI (now CNG powered) , 82 TD Caddy

Reply #3April 17, 2008, 04:13:33 pm

GoKraut

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Updated...got two of the four holes drilled.
« Reply #3 on: April 17, 2008, 04:13:33 pm »
Exciting business this is. Not only does it work in theory it works in practice as well.  I'm quite pleased I didn't have to take this thing out to put it in a mill.

Here are some pictures (again, they can be found on the link(s) provided above):








Reply #4April 17, 2008, 05:24:31 pm

GoKraut

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DIY fix for screwed up crank noses
« Reply #4 on: April 17, 2008, 05:24:31 pm »
complete success.





Reply #5April 17, 2008, 05:32:40 pm

jtanguay

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DIY fix for screwed up crank noses
« Reply #5 on: April 17, 2008, 05:32:40 pm »
and those 4 holes won't weaken the crank nose too much???  looks really interesting... that thing isn't going anywhere!!  :lol:


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Reply #6April 17, 2008, 06:38:29 pm

GoKraut

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DIY fix for screwed up crank noses
« Reply #6 on: April 17, 2008, 06:38:29 pm »
Quote from: "jtanguay"
and those 4 holes won't weaken the crank nose too much???  looks really interesting... that thing isn't going anywhere!!  :lol:


The holes are 5mm deep and the material for the crank is one hell of a lot harder than the cog.  Thats less than 1/4" deep.  Now I can't say this for sure because obviously I haven't driven it around yet but my educated guess is it will be just fine.   The thread for the crank nose starts at about 7mm into the crank. So as far as that goes it shouldn't weaken the mounting.

Reply #7April 18, 2008, 01:21:07 am

commuter boy

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DIY fix for screwed up crank noses
« Reply #7 on: April 18, 2008, 01:21:07 am »
I did a similar repair, but with just two holes.  As long as the key can't start moving due to the pins it should be fine.  Four holes looks like overkill to me.

Reply #8April 18, 2008, 03:36:43 pm

GoKraut

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DIY fix for screwed up crank noses
« Reply #8 on: April 18, 2008, 03:36:43 pm »
Quote from: "commuter boy"
I did a similar repair, but with just two holes.  As long as the key can't start moving due to the pins it should be fine.  Four holes looks like overkill to me.


I thought that originally too...but then I read other people's stories. First they tried one, then two.  Finally by the third it seemed to be OK.  There is a LOT of force that causes them shear in the first place - because on the one hand you have the crank bolt which is supposed to be around 77ft/lbs + 1/4 turn and THEN you have the 7mm key.  It takes a lot of force to shift the cog and shear off the key.  

And I do agree with you partly. The cog must not be permitted to move even a little.  I don't know if you've ever tried it but on a clean nose and new cog, there is very very little movement maybe one quarter of one degree.  Unfortunately that is why we're here.  Even that little amount of movement could not overcome those forces I mentioned earlier. The idea behind using 4 pins is pretty simple really.  Take equal loads across the geometric span of the cog - not in one or two places.

Though we'll see.  Believe me I don't want to be proven wrong here, not because of my ego - but because I just rebuilt everything and another failure would mean 3 cylinder heads.  :roll:

Reply #9April 18, 2008, 04:24:17 pm

jtanguay

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DIY fix for screwed up crank noses
« Reply #9 on: April 18, 2008, 04:24:17 pm »
Quote from: "GoKraut"
Quote from: "commuter boy"
I did a similar repair, but with just two holes.  As long as the key can't start moving due to the pins it should be fine.  Four holes looks like overkill to me.


I thought that originally too...but then I read other people's stories. First they tried one, then two.  Finally by the third it seemed to be OK.  There is a LOT of force that causes them shear in the first place - because on the one hand you have the crank bolt which is supposed to be around 77ft/lbs + 1/4 turn and THEN you have the 7mm key.  It takes a lot of force to shift the cog and shear off the key.  

And I do agree with you partly. The cog must not be permitted to move even a little.  I don't know if you've ever tried it but on a clean nose and new cog, there is very very little movement maybe one quarter of one degree.  Unfortunately that is why we're here.  Even that little amount of movement could not overcome those forces I mentioned earlier. The idea behind using 4 pins is pretty simple really.  Take equal loads across the geometric span of the cog - not in one or two places.

Though we'll see.  Believe me I don't want to be proven wrong here, not because of my ego - but because I just rebuilt everything and another failure would mean 3 cylinder heads.  :roll:


well vw over engineers their engines for a reason.  i think there is no way you're going to bust this off, unless the crank bolt somehow loosens itself completely, and then falls out, and even then i have a hard time seeing this setup fail due to the belt tensioning, unless the pins are loose enough.

good work! keep the diy coming :) its what owning a vw is all about  8)


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Reply #10April 19, 2008, 12:21:26 am

commuter boy

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DIY fix for screwed up crank noses
« Reply #10 on: April 19, 2008, 12:21:26 am »
The other thing to look at is making sure the end of the crank is perfectly flat to mate with the gear when it's bolted down tight.  My dad's been noticing some of them aren't exactly flat, which might cause more wobble, especially if a less than perfect torquing procedure is used on a new bolt.

If you're going to this much trouble, and you're that risk adverse I would have thought you'd pull the crank and machine a TDI shaped D on the end of the crank nose matched to a gear to a light press fit.

Do keep up posted as to how the fix works though, I'm curious.

Reply #11April 19, 2008, 12:52:35 am

GoKraut

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DIY fix for screwed up crank noses
« Reply #11 on: April 19, 2008, 12:52:35 am »
Quote from: "commuter boy"
The other thing to look at is making sure the end of the crank is perfectly flat to mate with the gear when it's bolted down tight.  My dad's been noticing some of them aren't exactly flat, which might cause more wobble, especially if a less than perfect torquing procedure is used on a new bolt.

If you're going to this much trouble, and you're that risk adverse I would have thought you'd pull the crank and machine a TDI shaped D on the end of the crank nose matched to a gear to a light press fit.

Do keep up posted as to how the fix works though, I'm curious.



Well the problem is I can't.  The TDI (and the like) use a different style belt that isn't compatible with the 16V and it wouldn't have been as cost effective to do that either.  Sadly I can only design, I don't have the tooling to manufacture so it required dinero $$$.  

...I thought of a better way of approaching the issue. Part two of the solution as a whole really.  The second part being a lighter "harmonic balancer" thankfully those DO exist in forms compatible with the 16V.  This setup is approximately 51% lighter than the stock pulley.  Since I'm not running anything but the stock load (electrically speaking), and I have no P/S and/or AC, the diameter of the pulley "harmonic balancer" shouldn't matter as much as it would in say those systems.

I posted some pictures on VWVortex which I'll just include in this thread here:

 
 
 
 
 
 

Reply #12April 19, 2008, 12:40:44 pm

jimfoo

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DIY fix for screwed up crank noses
« Reply #12 on: April 19, 2008, 12:40:44 pm »
That is just a pulley, not a harmonic balancer as there is no rubber or mass to dampen out the harmonics.
Jim
1966 Land-Rover 88" with 1.9 1Z which has been transformed to an M-TDI
TFO35 mechanically controlled VNT, IC , and 2.5" exhaust.
Driven daily

Reply #13April 19, 2008, 01:54:29 pm

GoKraut

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DIY fix for screwed up crank noses
« Reply #13 on: April 19, 2008, 01:54:29 pm »
Quote from: "jimfoo"
That is just a pulley, not a harmonic balancer as there is no rubber or mass to dampen out the harmonics.



That would be why it's in quotations.  :wink:

Reply #14April 20, 2008, 01:56:38 pm

jimfoo

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DIY fix for screwed up crank noses
« Reply #14 on: April 20, 2008, 01:56:38 pm »
Guess I missed them. :oops:
Jim
1966 Land-Rover 88" with 1.9 1Z which has been transformed to an M-TDI
TFO35 mechanically controlled VNT, IC , and 2.5" exhaust.
Driven daily