MrDave - thanks for posting your thoughts... I am still mulling and processing the information that you have contributed. (Edit: see below post for my reactions to these ideas.)
Mark the Miser - Re: thermal control for an engine lacking piston-oil squirters... I guess you missed the part of the plan which is to not set aggressive fueling levels. In any event, yesterday I ordered a VDO pyrometer to make sure the thermal limits are safe. I am planning on installing it pre-turbine into the exhaust manifold / turbine housing and will consider a red flag being raised if it approaches 1300 deg F (which is 200 deg. F cooler than the factory 1.6lTD.) I also never said I wasn't planning on running an oil cooler, or a TD fuel pump. (I was only in question about which type of oil cooler to run. I'm leaning towards the factory version at the moment by the way, mostly due to the fact that I already have it, and that it might be hard and expensive to track down a thermostatically control sandwich plate which I'd want if going external oil cooler route.) Also, re: your contention that the crankshaft differs between an '84 1.6lNA vs TD, show me some evidence that supports this notion, because according to ETKA as discussed on this board already, they have the same part number. I am planning on installing the TD harmonic balancer pulley.
I also wanted to update you all on where I am with the VNT can...
I first took some more measurements to determine the viability of my idea that wouldn't require modification of the can. I found a vacuum gauge in the shop that I could use so I can measure actual vacuum values, rather than estimate them from diaphgram area and forces.
The vacuum pump (this is an '84 Rabbit, with the compact vane-type vacuum pump not the diaphgram style by the way) pulls a very healthy -29 in Hg (that's -14.2psi.) Although that is for zero air flow, and I found that the vacuum strength gets weaker as flow increases.
The actual, as-installed amount of vacuum necessary to get the VNT mechanism to begin closing is -7.5 in Hg (-3.7 psi). -17.5 in Hg (-8.6 psi) is required to reach full closed. Then due to friction in the mechanism, the valued required to get the vanes to open are different: -16 in Hg (-7.9 psi) required for it to begin opening, and -2.0 in Hg (-1.0 psi) required to reach full open.
Putting all these numbers into my spreadsheet I built to predicts the vane movement for various boost levels and R2/R1 relationships, I found I'd need an R2/(R2+R1) to be 45% or less to make the vanes remain fully closed after the engine is started up when there is zero boost, and 40% or less to make the vanes return to fully closed after the engine has gone through a boost cycle.
At 45%, the vanes would reach full open at 15 psi, and wouldn't start to begin closing until boost dropped below 10psi.
At 40%, the vanes would reach full open at 19 psi, and wouldn't start to begin closing until boost dropped below 12psi.
I was hoping that there may be a relationship that would allow the vanes to be completely closed, and then open the vanes over a tighter boost range.
What does this mean? I decided I am not confident this scheme would reliably control the vanes in a narrow boost range. There is risk that this method may give boost creep, due to the wide range of boost pressure change necessary to get the vanes to move from full close to full open, and vice versa. And I'd rather not install the turbo with everything hooked up to find that it has to come off because I need to open up the can.
Result of this... gave me another reason to make the can open/closeable, and assess the viability of QuickTD's idea to convert the can from vacuum to pressure. Using a grinder, I thinned the metal around the outside rim or the crimp, and then I finished off removing the crimped on ring by carefully chiseling it off. After filing off any remnants of the crimp ring missed by the chisel, so there was nothing left to hold the can closed, I gently pryed the can open. For modification of the diaphgram to take boost rather than vacuum, I think the diaphgram will need to be flipped over along with it's rigid metal support behind it, to keep the metal support on the low pressure side and prevent the diaphgram from "balooning". To flip the diaphgram required that the linkage rod be removed (which was permanently riveted on.) The flipped over can with spring on the other side will have less room in the can to move around, due to the can and the diaphgram support being different on one side versus the other. However, I think there would end up being enough travel to completely move the vane mechanism, if the linkage were tuned correctly. I bought some various 6mm studs, threaded on both ends with a smooth center area, to experiment with replacing the riveted on linkage rod. I was able to install them to the diaphgram using nuts on either side of the diaphgram. I first tried a stud about 3" long but found it was too long, so went one step shorter. If I need to change anything, IE the rod length, change the diaphgram or can somehow to change it's travel of the spring pre-load, or change the spring, I wanted the can to be serviceable by just undoing some bolts, but I wanted it to also seal reliably.
I set about solving the problem of finding a clamping ring to seal the can back up. I bought a 4" wide plate of thick aluminum. And using my new dremel tool with router attachment that can do circles, I already precisely dremeled through a hole through the thick aluminum that has the needed 2 5/16"ID. My next step may be tricky, but I want to try and machining a relief in the edge of the aluminum, so that a shoulder sticks out past the outside of the can, so that the bolts I'm going to install holding the can together have a shoulder on the outside so they are evenly tensioned and not torqued.
I'll post pics of it later if I am successful, with me luck!
(If not, DVST8R, maybe I'll shoot you the details specs of the piece I am trying to fabricate and take advantage of your offer.) I am planning to clamp the can together with either 6 or 8 little bolts (6mm with wide bolt head).
PS - although I haven't taken any measurements of the pressure required to get the modified can to move the VNT mechanism, I did (with the can clamped together with a couple c-clamps) apply some pressure to the uninstalled can and determine the pressure required to move it's linkage. The results so far are encouraging. The resulting range to make the linkage start moving and reach full travel are: 6-7 psi to start moving out, and 10-12 psi to reach full extension.
I hope the range to actually pull the VNT mechanism open and closed is somewhere near this tight!
I can always plumb in a bleeder valve if I want more boost pressure, so I was glad to see some pressure numbers that were in a reasonable or maybe slightly low range (I'd like to eventually target running around 10-14 psi boost level on this thing.)